Jason left Cribbit by bridge 200 and I set off for Stoupa, so no way for me to even find out what could be wrong before I got back. Once I did had a quick look round and all seemed OK although there was no coolant in the system. Decided that I would check the weed hatch first as a few polythene bags round the prop soon causes the engine to overheat. Sure enough the prop was well fouled. Started filling the cooling system, and it did seem to be taking a lot of water, then the automatic bilge pump started up and I decided that the water might well be going in but seemed to be coming back out again just as fast. Quick check of all the core plugs, all ok, so where? Checked the hoses and realised that the main return from the skin tank had sheared off completely. Measured it up and set off to Uxbridge marine for a new length.
Fitting the new hose was a simple job and soon completed. Filling the cooling system not so quick as it seemed to be taking a prodigious amount of water, so much so that I thought that perhaps there was another leak, but how to tell? I had opened the skin tank stop cock to allow air to escape so what could be simpler than a bit of fairy liquid over its end to see if it would blow bubbles?
Soon had the engine running again and by then had had enough time to cogitate on my next move. Well as we are half a day away from Northolt, we may as well continue on North and get the reconditioned engine I have been promising her for years. So turned her round and headed back towards Cowley lock. The next day got me comfortably to Copper Mill lock where I was hoping to see the bats as in former years. Thwarted in this but that is the next episode.
After I had moored up at Copper Mill, I did my usual system check and noticed that the 'alternator was a bit wobbly' so knew that this would be the first job to do next time I wanted to move on. As it happened, it was tw who was to move her on next so this became HIS job!
What better initiation to the joys of boating could there be for Tanya?
Moved Cribbit on from Red Lion Lock [69], through Hemel Hemstead and moored above Fishery Lock [63]. Not many pics as single handing.
A bit of boating and then a couple of days of angle grinding and anti-rust coating. Engine and angle grinder getting a bit hot, the engine because the plastic header tank failed with high pressure steam spurting from a large crack in its side. Soon stopped this with a good application of duck tape.
Weather warm, so warm in fact that it was impossible to put bare flesh on the roof. Used the roof washing water to keep my knees wet but no such easy solution for the rustproofer so had to balance on the hand rails.
to follow
The demise of the cooling system header tank finally pushed me into a long overdue overhaul of the cooling system which has been promised for some time. Out came the 'organ pipes' a desperate measure to increase the cooling area embarked on when I was at Solihull and hand crafted for me by the refrigeration department. These were made redundant after I had a new skin tank grafted onto the outside of the boat that contained baffles to stir up the cooling water. A very necessary modification needed for lengthy Thames passages at high engine revs.
I got a replacement header tank from the breakers yard in Oakley [£4] and then a trip into Apsley to the very good motor spares place on the High Street where I was able to buy heater hoses to hook it all up.
Decided that I would mount this item above deck. Quite some debate about whether this was a good idea or not. Against was the possibility that it would be used as a step but the big plus was that I could keep an eye on it. Then I wondered why cars aren't fitted with little windows so their tanks can be observed too. Decided that I already knew the answer to this. Another plus was that it gave me a handy place to mount the engine cut out lever as well. [Of course if you want to stop the engine because steam if coming out of the tank, this might not be the best place for this...ahhh well]
Got some undercoat on the roof and ran the engine for an hour or so so felt fairly confident about the engine for my next set of visitors who were to take cribbit on her next stage. This fell to Ann and David who moved her on to Cheddington though not before experiencing a small fuckle or two. Well the cooling system seems to have worked quite well but that a core plug failed but was expertly bodged by David with silicon gasket goo. They also found the only thunder storm in the region, not experienced by us 30 miles away.
Now I thought that replacing the core plug would be quite easy, after all I had several in waiting on board, alas these were all the wrong size so deciided another trip to Apsley was in order. The shop had lots too but these were all the wrong size as well. The motor world has gone metric since that engine was made. Eventually found one, almost the last in a large box of the things. Well it was right for one axis of the original but a bit big for the other. Sure enough, when I got it back it didn't fit either, even with a bit of persuading. No matter lots of that gasket stuff left, for now, and we were soon up and running even though I didn't dare pressurise the system.
Before heading to Apsley, I came across a fisherperson delving into the canal with a fish net. Asked him what he was about and he explained that the previous day he had dropped his tackle in the cut and that he was hoping to recover some of it with the net. Got out the fishing magnet and showed him how to use it. On his first attempt he recovered two red handled objects which pleased him greatly. That's my bait threader and my knot picker he exclaimed, that has saved me at least £5! Anyway, I was in a hurry so said to him to just leave the magnet in the bows of the boat when he had finished with it and off I went to Apsley motor spares . When I got back found my magnet as arranged but also a nice [if slightly muddy] armco hook. Magnet fishing can be so rewarding!
Spent the rest of the day moving down to Grove Lock and its pub.